Okay, I used my GX CS4 compressor to top of my 6.8L tank the other day and ran it for about 30 minutes or so to top off the tank at 300 bar. As you may have guessed, I’m a tinkerer and am always curious how things work. So, I looked at the CS4, it looked at me and I removed the case.
It’s really easy to do – I removed the little sheet black metal screws that run around the edges of the red sheet metal cover, removed the coolant tank cover, unfurled the power cord wrapped on the spool and the cover just comes straight off.
Here are some photos:
Summary
The design is well executed – everything is neatly assembled and the pump continues to work great. There are probably over 5-6 run time hours on it so far.
Here are the GX compressors from the CS4 down to the CS1
FastToBuy 30Mpa Oil Water Filter – Not a GX product but I recommend this filter and you need one between the compressor and your tank or PCP airgun. You will need an extra hose from it to your tank or airgun plus the proper fittings.
Note, I have to buy all of my parts – nothing here was paid for by sponsors, etc. I do make a small amount if you click on an ad and buy something but that is it. You’re getting my real opinion on stuff.
If you find this post useful, please share the link on Facebook, with your friends, etc. Your support is much appreciated and if you have any feedback, please email me at in**@ro*********.com. Please note that for links to other websites, I may be paid via an affiliate program such as Avantlink, Impact, Amazon and eBay.
There should be a small pamphlet in with the CS4. Take a minute and read the instructions for use. Afterwards read the following.
Distilled Water or Antifreeze for Cooling?
So the pump gets its really long duty cycle in no small part due to the liquid cooling system. Liquid is a far, far more efficient conductor of heat than air is. You see, water is much more dense than air and depending on the article you read it is 9 to 13 times more efficient at carrying away heat – maybe even more.
In the automotive world, to lower the freezing point and raise the boiling point, various chemicals have been discovered and are often referred to generically as “antifreeze”. You look deeper though and there are tons of variations for different manufacturers and different specifications.
GX said to use either distilled water or a PH-neutral antifreeze. Well, I wasn’t sure how hot the pump would get so I was worried about using distilled water. The benefits of distilled water is that it is cheap and it is PH neutral being neither acidic nor alkaline so it’s not going to cause excessive corrosion. On the other hand, it can freeze or boil like any other water plus there aren’t any corrosion inhibitors or pump lubricating agents.
I was very keen to use an antifreeze for longer life plus I was worried about boiling. I didn’t plan to keep the pump outside so freezing wasn’t a worry. The problem began when I tried to find “PH-neutral” antifreeze. I could not find any antifreeze with a true PH of 7. I turns out that you will be hard pressed to find it – I found cutting fluids (coolants for doing metal cutting) with a PH of 7, brake line antifreeze that had a PH of 7 — it was almost pure methanol, but not a thermal transfer fluid that I could buy in small quantities (like 1-2 gallons).
The more digging I did the more I realized that I could use an automotive antifreeze but needed to find one with a relatively low PH (7-9) and also that contained corrosion inhibitors and was aluminum and plastics & hose friendly. To make a long story short, this led me to Valvoline’s Zerex G48 coolant and I opted for a 70/30 mix of coolant to distilled water. My local Napa autoparts store was able to order in a gallon jug with same day in store delivery. It’s a fortune to mail order but only $14-17/gallon at a store.
Do not add it to the unit yet! You will need to test and flush the cooling system first
Powering It Up
Before you get to far, plug the AC-to-DC adapter in the wall. You should hear the cooling fan turn on — it definitely needs it so if you don’t hear the fan make sure there is AC power through the power cord to the adapter. There isn’t an on-off switch – the unit should turn on as soon as you plug it in.
Put a multimeter on the power supply terminals and you should see around 13 volts. My CS3 power supply is 13.16 volts and the CS4’s power supply which is the same model just newer measures 13.06 volts.
Make sure the CS4’s switches are off before you connect the compressor to the power supply.
Flushing the Liquid Cooling System
The nut with viewing glass that covers the water tank should just be on hand tight. If you must, use a wrench to remove it but just put it on hand tight when you re-install it going forward. The system is not pressurized – you can take the cap off while it is operating.
For some reason my CS4 shipped with a little bit of water in it – maybe from testing at the factory and there was also some kind of brownish sediment on the bottom of the “water tank”.
The liquid had no smell and felt like water – I have to guess it was water so I just dumped it out. I then refilled the tank with clean distilled water and swirled it around. I did this four times until the water stayed nice and clean.
For testing and flushing the system, just use distilled water. It’s cheap and doesn’t make a huge mess if there is a problem or something spills. Been there, done that – use water – trust me. By the way, purified water may not be distilled – the purified water might just be filtered. Distilled water uses a process that not only purifies the water but has the minerals removed as well. You don’t want minerals to leave a scaly buildup so use distilled.
I then turned the unit on and watched the water – nothing happened. There is a water pump – the intake is in the center bottom of the tank and the return is on the side about 3/4ths of the way up – there was no water moving. Oh man … I started to get really worried that maybe the water had frozen and snapped the pump but everything was dry when I took it out of the box … but …. stuff happens.
I started to take the case’s screws off to look inside. At one point, I leaned the unit part way over to get to a bottom screw and heard the familiar “glug glug glug” sound of water running into a void that previously had air in it. That was a very, very welcome sound because it dawned on me that the little water pump had lost its prime.
I looked at the water tank and the water level had definitely gone down. I turned on the pump’s main switch and the pump started moving the water! Lesson learned there – prime the pump.
The next thing was that brown sediment was entering the tank as the lines blew out in the unit. I then dumped out the water and flushed the lines three more times until everything looked clear. Each time I would wiggle the compressor around leaning it slightly from side to side and front to back until the pump would prime. You fill the water tank to the bottom of the return line. This gives room for the coolant to expand and it also gives you a visual cue if the pump is working.
Now this told me something – there would be more water in the unit than just what was visible in the tank. In the instruction pamphlet they say you need to add 500ml of liquid to the unit. The unit came with some amount of water in it and each time when I drained the unit, I was only adding back in about 130 ml of water each time – I was using a 1000ml graduated cylinder for all of this. So, 500-130=370ml of trapped water in the system. Hmmm…. this was throwing my planned antifreeze ratios all off. 500ml of fluid at a 70/30 ratio would mean 350ml of antifreeze and 150ml of distilled water. I was going to be off and you need enough water in an antifreeze for the chemicals to move around properly.
In general, 100% pure antifreeze concentrate is a bad idea – there is a ratio you need to follow either based on the temperature range you need or what the vehicle manufacturer recommends. With G48, most vehicle makers recommend a 50/50 mix and there is actually a premixed formula with a typical PH of 8.1 (the range is 8-9). I was going for 70/30 to have as low of a PH as possible (pure G48 has a PH between 7.1-7.3) and to maximize corrosion protection.
Well, the trapped water was throwing a wrench in my plans because I had already mixed the 70/30 not realizing I would have a bunch of extra water in the jacked and lines. Rather than drive myself nuts, I decided to go ahead and test the unit by draining out whatever water I could my tilting/moving the machine around while it was upside down and then refill with 70/30. After testing I will drain the tank get the antifreeze ratio closer to 70%.
I was not able to collect the final PH at this time. My test strips are absolutely useless with the dark blue of the G48 fluid. A friend has a calibrated digital tester that we will use some time in the future.
As I was writing this blog post, I was talking to my friend John, who is a master mechanic and has forgotten more than I will ever know, and told him about this. He didn’t even have to think about it – he said “pull a vacuum through the inlet or return and drain the system”. Duh. He was spot on – I sure hadn’t thought about doing that.
I used a MityVac MV-6830 brake line bleeder to suck all of the liquid out through the inlet. I put 70/30 in the tank and used a right angle adapter to pull all of the fluid that way. I then refilled the tank with 70/30 and pulled just enough vacuum to the point I saw fluid entering the hose and stopped – I did that last part to pull fluid into the pump.
I then turned on the master switch so the fan and water pump would start. Nice clean 70/30 G48 was coming out. I slowly added more mix to the tank until I got to the bottom of the return line. I had to top it off just a tad maybe 2-3x as fluid filled little pockets. I let the unit run for another five minutes and when the fluid level stayed the same, I put the cap back on – done. It helps to have smart friends.
Here’s my lessons learned that I want to share when it comes to the cooling system:
1. Flush the cooling system out using distilled water and then use a vacuum bleeder or siphon tool to more fully drain the system. I put put about 250-350ml of fluid to fill the system in the end. The important thing is to fill the tank to the bottom of the return.
2. If you don’t see the fluid moving, you most likely need to prime the pump either by moving the CS4 around to work fluid down into the pump or draw it into it using a vacuum bleeder.
3. Test the cooling system with water – not antifreeze or you will make a mess plus water is cheaper.
4. While you can use distilled water, I would recommend Zerex G48 at either 70/30 or 50/50. I went with 70/30 that I had to mix from the concentrate.
Testing the CS4
Now that the critical coolant discussion has been addressed and you have filled the unit accordingly, let’s switch gears and start actually testing the unit. After every test, drain the unit using the bleed valve. I will bring this up again later but do not attempt to start the compressor with pressure already in the line.
There will be some very high pressures involved. If a fitting does not want to come off, STOP. Many times a quick release collar will not move or a threaded fitting turn because the line is pressurized. Always make sure the line is depressurized before you work on it, remove a fitting, etc.
Each bold heading below is a test I would recommend that you perform and if it fails, stop and contact the Amazon seller – Ankul. I am not a representative – just a user. With that said, here are the tests:
Make sure the fluid pump is running
Before you start pressurizing the system, again, turn on the master red switch but not the pump. You should see the coolant circulating, If you do not, try moving the unit around to get the pump to prime
Turn the compressor on with nothing attached
With the airline off and just the male foster fitting exposed with nothing on it, turn on the pump by pushing the top silver button. You should hear the pump start and feel air blowing out from the end of of the foster fitting rhythmically – there is a piston so the air will come out as the piston pushes upwards – it is not a continuous flow. You should not hear any awful grinding noises or banging sounds. Slight squeaks as things start to lubricate and wear in are possible – you are listening for “OMG – what the hell is that?” sounds.
Let it run for a minute or two and if no scary sounds start then shut off the compressor.
Test with the supplied pressure hose only
To test high pressure air systems, always pressurize incrementally starting with the smallest thing first and work your way up to larger and larger volumes. In this case, start with just the air hose attached.
This is our first real test of the compressor under pressure plus we get to check the hose assembly. With that said, connect the air line and insert the test plug in the end. Make sure the plug is fully seated. Also, make sure the drain valve / pressure relief valve is closed – this is the black knob on the front of the unit. Clockwise closes the valve – it screws closed basically.
Set the limit switch / stop switch on the top to 300 bar. Put the secondary switch at 310/320 bar. I put my second switch just before 400bar but in hindsight, I would tell you to put it around 310/320.
Turn on the compressor by pushing the silver button. You should see the pressure build very quickly – the manual says it should reach the target 300 bar pressure in 38 seconds. I think mine was a bit faster than that.
Now, don’t do a thing. Watch the pressure gauge. It should just sit there – if it is going down there is a leak. The most likely culprit is the drain valve isn’t fully closed. Wait until it leaks all the way down or open the bleed valve to speed things up. You don’t need to go crazy tightening the valve knob as you are liable to hurt something but it should be firmly closed. Make sure it is snug and try again. 90+% of the time that fixes the issue.
If it still leaks drain the system, remove the test plug and look in the female foster fitting – is the rubber o-ring still down in there? Same goes for the other end of the hose that plugs into the machine. It could be missing. So, if it is, insert an o-ring and try again. If the o-rings are there, sometimes just removing and reseating a quick connect fitting/plug can solve the issue. Make sure the bleed valve is closed and try again. If it will not build pressure, contact Ankul on Amazon.
Soapy water in a spray bottle can help you find where the leak is at. Do not run your hands right against the fittings or you risk air getting injected into your body and that is very bad.
By the way, I let mine sit for about 3-5 minutes before I decide. Usually a leak is really obvious in the first minute – the first few seconds even. Either it will not build pressure at all or it leaks down fast.
Bleed off any residual pressure. Opening the bleed valve also allows any trapped moisture to blow out of the drain line also. I doubt you will see it with this short of a test but you will sooner or later so don’t worry. It’s supposed to do that.
Test with the filter installed
Assuming the pressure line passes testing, it’s time to up the volume game and pressurize the air line and whatever external filter you want to run. I am using a big 300mm long filter with a 50mm outside diameter sold by FastToBuy on Amazon. Yes, the CS4 has an internal filter – but I really want the air to be dry.
First, make sure the system is depressurized by opening the bleed valve. Then plug your filter into the air hose and this time put the test plug on the end of the filter. All of your fittings should fit together very nicely. If you find something doesn’t want to go together, stop. Buy a replacement fitting, I like Air Venturi brand but any reputable brand will do. I’ve had Chinese no-name filters, hoses and other items with out of spec fittings that will not go together. Last month, I had a brand name fitting whip off a Hatsan Jet II and hit me in the glasses so hard that the polycarbonate lens was gouged and my glasses were flattened against my face on one side – I had tried to push the fittings together and they didn’t mate properly. Moral of the story – fitting should go together easily without forcing.
Once the assembly is together, the bleed valve is closed, set the pressure limit switches to 300 and 310 bar then turn on the compressor. It may take it a minute or two for enough pressure to build up to show on the pump’s pressure gauge. It may take a few more minutes depending on how big the filter is before it reaches 300 bar. As before – stop and watch the pressure gauge, it should hold steady and not leak down. If it does, then check the bleed valve, o-rings, etc.
The absolute most common source of leaks is at the fittings – worn or missing o-rings or one fitting not really sealing well against another and you then need to decide which fitting to replace. Soapy water in a spray bottle can help you find where the leak is at. Do not run your hands right against the fittings or you risk air getting injected into your body and that is very bad. Notice the repeat on that safety comment.
If everything passes, open the bleed valve to dump the air in the filter and line.
Time to Fill The Tank
Part of my push for the new CS4 was to also fill my new 6.8L 4500 PSI Airmarksman tank. I really wanted to go with a new Omni or Patriot (US made Omnis) but the 6.8L model is hard to find so I went with Airmarksman because I really wanted two gauges – one with line pressure and the other with tank pressure. Standard single gauge units just show you line pressure.
It’s nice, the Air Marksman’s air hose attaches via a quick connect. I can go right from a female foster fitting on an airline right into the tank – no more little male-to-male quick connect fittings that are easy to lose.
I also bought a really nice 3′ long Manloney air hose extension to go from the new filter to the tank. In general, I am not a fan of hanging a filter right on a fitting because you create a long lever arm that is too easy to snag and break. Instead, I prefer a hose to the filter and then a hose from the filter into the tank.
You know what this means right? I tested the Manloney hose extension by inserting the test plug, and doing everything we’ve talked about previously.
I then bled the air off and let the unit’s cooling system run until the exhaust temperature was the same as surrounding surfaces because it was time to get real. Filling the tank from empty to 300 bar would take at least 2.5 hours and I wanted to record times, pressures, temperatures and and decibel readings along the way.
I couldn’t just sit next to the compressor and tank for the 3 hours and 22 minutes the test was running. I set the shut off on the pump to 300 bar but what I found was the needle you are moving around to shut off the pump is not precise. For example, I wanted 300 bar but what I got was 257 bar of 3,725 PSI. I then ran the unit another 10 or 15 minutes to take it up to 300 bar even and then moved the limit switch / shut off needle slowly backward until it stopped. Now the first switch is set where I want it. The second need is just behind it by about 10-20 bar.
The temperature management is remarkable. I was using a very good Fluke infrared thermometer to measure the exhaust fan area’s temperature and once it got up to about 100 degrees it pretty much stayed there once the unit warmed up. The noted coolant temperatures were collected by me removing the lid of the water tank and using the Fluke infrared thermometer to get a reading.
Speaking of temperature – this ran far cooler than I thought it would. I actually thought the fluid would get hotter and risk boiling. I still like using antifreeze for the corrosion protection and lubrication of the pump but boiling is not a concern and I don’t foresee it ever being some place where it could freeze but I guess lowering the freezing point is a good idea just in case.
In terms of sound, the unit turned on with just the fan and coolant pump running is 71DB according my BAFX 3608 decibel meter. The sound level with the compressor running was in the 82-84DB range about 8-10 inches from the side of the unit – not bad at all. I thought it might get louder as the pressure increased but it didn’t.
Last comment – the unit ran for well over 3 hours and thirty minutes – probably more like 4-4.5 with all of the testing. There were no funny sounds, no unexplained leakages, etc. That amount of running gave me a real good impression of the unit. After all of that running, I did turn the grease pot one rotation.
Special Note: DO NOT Start or Re-start The Compressor Under Load!
GX stated in multiple places to not try and start the pump with the system pressurized. I imagine it puts too much strain on the electric motor and other parts to get spinning. When I did the top off fill mentioned above, I closed the tank’s valve and opened the bleed valve on the compressor to depressurize the line. Unsurprisingly, maybe a teaspoon or two of water came out as well. I then closed the bleed valve, started the compressor and after it came back up to speed only then did I re-open the tank valve and put the system back under load.
By the way, I am not surprised by this at all. With shop air systems, part of the pressure limit switch is to also open a bleed off valve to depressurize the pump. It’s fairly common for these switches and valves to wear out. If the air doesn’t bleed off then a breaker may trip given the increased load. So, giving the CS4 a chance to start without a load and come up to speed first makes sense to me.
Summary
I was really impressed by the smaller CS3 model that I have used since November 2020. I bought this new CS4 model because I had such a good experience in fact and now that I have run the CS4 over four hours, I’m pretty happy. The CS4 will fill the niche in the GX line-up for a medium-duty machine for 6.8 Liter and smaller bottles. The CS3 will continue to be sold for people filling 1.5L or smaller cylinders.
Wrapping up – I really like the unit so far and will definitely post updates as time goes on.
Here are the GX compressors from the CS4 down to the CS1
FastToBuy 30Mpa Oil Water Filter – Not a GX product but I recommend this filter and you need one between the compressor and your tank or PCP airgun. You will need an extra hose from it to your tank or airgun plus the proper fittings.
Note, I have to buy all of my parts – nothing here was paid for by sponsors, etc. I do make a small amount if you click on an ad and buy something but that is it. You’re getting my real opinion on stuff.
If you find this post useful, please share the link on Facebook, with your friends, etc. Your support is much appreciated and if you have any feedback, please email me at in**@ro*********.com. Please note that for links to other websites, I may be paid via an affiliate program such as Avantlink, Impact, Amazon and eBay.
Life is a funny thing – I grew up with firearms. Yeah, my dad had these two old pump action Daisy airguns that were fun to shoot tin cans with but starting at a pretty early age I liked things that went “bang”! Sometime in the early 2000s, I got back into airguns to deal with pests. I started hearing about a class of airguns called “pre-charged pneumatics” (PCPs) that used 3,000 PSI high pressure air cylinders somewhere on the rifle to propel the pellet. They were reported to be accurate, reliable and capable of rapid repeating fire through through the use of a manually operated bolt and a magazine.
I thought that sounded so neat – especially the rapid follow up shots. What stopped me from buying one was that they had to be refilled from a SCUBA tank that was filled at a diving shop. Well, I eventually found out there were specialized hand pumps and you didn’t need to spend a fortune on a tank and hassles with going to the dive shop. I bought a Hill Mk.4 hand pump along with a .22 Hatsan Gladius Long that I used for a few years.
I wrote a post about buying it and also one about setting it up and testing it. I almost always used the CS3 to top off a really nice little Omni 18 cubic foot tank that I would then use to fill my growing number of PCP airguns. It really worked well – the tank was really convenient to pull out and top off an airgun and I would only occasionally need to bring out the CS3. Sure, I could have filled the airguns directly from the CS3 but I wanted to keep things simple.
Fast forward to January 2023 – I bought a .30 Umarex Gauntlet with a big cylinder and was planning to get one or two other high air consumption PCP rifles in 2023 so I started thinking about how to feed them. It was a total coincidence that GX unveiled their next generation CS4 compressor on Amazon. There were just a few four or five reviews at the time and I decided to gamble on the new pump and bought it on January 29, 2023. I took the leap because I had such a positive experience with the CS3 and I knew I could return it to Amazon if it turned out to be a problem child. [Yes, I bought this so you are getting my honest observations – click here for the Amazon CS4 product page.]
On January 31, 2023 the Amazon driver brought be a big heavy cardboard box with the GX CS4 and I started getting my stuff together to do some testing plus a time slot to fill a big 6.8L carbon fiber tank from empty to 300bar which would take 2-3 hours I figured.
Now, I’m going to tell you something – it is slick. It is really, really slick. I’m telling you this so you take the time to read more in this post plus one about setting it up and testing it.
What is the GX CS4?
The CS4 is an additional pump offering from GX for people wanting to fill larger cylinders than the CS3. It also reflects design advancements to the CS3 unit – here are the features that really caught my eye:
CS3
CS4
Working Pressure (Mfg supplied)
30MPa/300 bar (4,351 PSI)
40MPa/400 bar (5,801 PSI) – 33% more pressure
Air volume (Mfg supplied)
7 liters/minute (0.247 cubic feet/min)
11 liters/min (0.388 cubic feet/min) – 57% more air volume output
Suggested Maximum Air Cylinder Size
2.5 Liters
6.8 Liters
Cooling
Air with fans
Coolant with radiator and fan
Power (Mfg supplied)
12V 250 Watts
12V 350 Watts – 40% more watts
Duty Cycle (Mfg supplied)
30 minutes working and 20 minutes cooling
5 hours continuously working. Manual says to let it run for 1-2 minutes after pumping is complete – 10x longer duty cycle.
Sound Level (Mfg supplied)
75db
70db
Pump lubrication
Not needed (until it slows down – mine hasn’t so far)
Has a grease pot to add grease every 4-6 hours of run time
Limit switch
Simple rotary dial limit switch
Protected twin pin design where you can set both the limit and failsafe limit
Hose
19.6″ permanently attached hose
19.6 hose that is removable via a quick connect foster fitting
Weight (my digital scale)
19.4 pounds
29 pounds with antifreeze – 55% heavier
Dimensions (me with a tape measure)
5-3/8″ wide (about 5-7/8″ wide including the wire spool on the side) x 9-1/2″ deep (10-1/4″ if you include the release valve) x 10-1/2 high at the top of the case (about 11-1/2 overall if you include the handle)
6″wide case (6-1/2″ wide with the wire spool) x 11-78 deep (12-3/4 if you include the release valve) x 12-1/2″ at the top of the case (about 13-1/2 at either the top of the grease pot or the folded handle) – about 62% larger overall
For me, the really long duty cycle is what I was looking for. The 57% increase in air output is a welcome enhancement to have over the CS3. Since I would fill my guns from my tank, I was never in a rush. Now that I have 6.8L tank, the fills will probably be less often but a lot more volume will be needed so it’s good to get that increase.
The increase in air pressure is overkill right now – there aren’t affordable 400 bar working pressure tanks as of yet – they are out there for specialty applications but are in the $1,500-2500 range. I’m sure the price will come down over time but most carbon fiber air tanks that PCP shooters are using are in the 300-310 bar working pressure range. If you see 400 bar, read the ad again because they may be talking about the test pressure and not the working pressure – you fill to the working pressure only – never to the test limit.
To be clear, the GX CS4 is not replacing the CS3. They have added the CS4 to fill larger tanks faster. They identify the 6.8 liter tanks as being the target max size for the CS4 and for me the duty cycle is the more important number. You can fill anything you want as long as you don’t bake the pump.
With the CS3 for example, the 20 minute duty cycle is what limits a convenient tank size. If I needed to fill my Omni 100 cu in (1.64 liter) tank from empty – I would let it run for 20 minutes and then I would stop the pump but let the fan run until it cooled down to room temp. I’d then close the cylinder valve, bleed the air out of the line, start the air pump again and as it came up to speed I would open the cylinder’s valve again. It took a while but it worked just fine. I tried to always be mindful of the duty cycle and give the unit a chance too cool down before I either shut it off or resume – I’m sure that’s one reason I’ve had zero problems with the CS3 since I bought it.
FastToBuy 30Mpa Oil Water Filter – Not a GX product but I recommend this filter and you need one between the compressor and your tank or PCP airgun. You will need an extra hose from it to your tank or airgun plus the proper fittings.
1/28/24 Update: Had to fix Amazon links so they work in the list above the summary. I’m still using my CS4. No problems.
6/12/23 Update: Fixed the wording about being conservative. Thanks KG!
Note, I have to buy all of my parts – nothing here was paid for by sponsors, etc. I do make a small amount if you click on an ad and buy something but that is it. You’re getting my real opinion on stuff.
If you find this post useful, please share the link on Facebook, with your friends, etc. Your support is much appreciated and if you have any feedback, please email me at in**@ro*********.com. Please note that for links to other websites, I may be paid via an affiliate program such as Avantlink, Impact, Amazon and eBay.
The ATF conducted a webinar on 1/31/2023 to help FFLs understand the new brace rule that went into effect that same day. That means anyone with a braced pistol needs to decide what course of action they are going to take because they have 120 days to comply.
Unless someone gets a temporary restraining order issued to put a hold on this regulation, people must figure out what they are going to do and when. Please notice I said “and when”. Figure out what option you are going to take and when you must start doing it. For example, if you plan to remove the brace and destroy it, when must you do that by? If you plan to make your pistol into a rifle, when do you need to order parts and do it by? Always remember that a whole bunch of other braced pistol owners will wait to the last minute and then get upset when they can’t find parts, their gunsmith doesn’t have time, etc.
Click here for the ATF page that links to all of the published guidance they have involving braces including the full text of the new rule and frequently asked questions.
If you find this post useful, please share the link on Facebook, with your friends, etc. Your support is much appreciated and if you have any feedback, please email me at in**@ro*********.com. Please note that for links to other websites, I may be paid via an affiliate program such as Avantlink, Impact, Amazon and eBay.
We still have to see what the ATF continues to try and clarify. They have said 922r does not apply and they also said the 88 day background check issue still applies so keep tabs on things.
It’s really an unsettling unsettling time for owners of pistols with braces to be in. The four options in my own words:
Remove the brace and go back to having just a pistol. Destroy the brace.
Turn the pistol into a rifle either changing the barrel to over 16″ or adding an extension. Remember the 26″ minimum overall length limit.
Go the SBR route and register your weapon. Bear in mind selling it down the road would require working with an 03 FFL and not a basic FFL.
Turn in your braced pistol to the ATF to destroy it (I hope nobody has to go that route.
Speaking for myself, I’d either go for #1 or #2. If you’ve always wanted a SBR, then go that route.
Now that the timer is running and the ATF had a webinar for FFL dealers today to try and explain what is going on, I guess we will find out more.
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A number of years back, Toyota decided to move from the old spin-on canister-type oil filters to the use of cartridges encloused in a housing. The cartridge is really just the filter element so that’s what get’s tossed, burned, recycled or whatever and the housing is re-used. The problem is that they made the cap of the housing out of some form of polymer and it can crack or chip over time.
In the case of my daughter’s 2013 RAV4 XLE, the polymer cap was chipped near the bottom (closest to the road) and was starting to crack. We bought it when it was returned to the dealer at the end of a lease so who knows who was doing the oil changes or how much they cared.
At any rate, it puzzles me why Toyota went with Polymer. Maybe they wanted to to be softer than the aluminum. Maybe it was cheaper …. not really sure. On one hand you could validly argue that the cap lasted almost 10 years. On the other … it’s polymer and can crack. After asking around, friends recommended I move to an aftermarket aluminum housing to avoid future problems.
RJSPHH figured out that by having the same cap and different filter tubes internally, they could cover quite a few Toyota oil filter caps for Avalons, Camrys, RAV4s, Tacomas and more – you actually need to go to their Amazon listings to see all of them. The Toyota oil cap part numbers this particular model can replace are:
I’d recommend you confirm the part number your vehicle uses by looking up the part number on the Toyota parts website or by using your favorite parts website. This way to can verify both by year and model as well as the OEM filter canister part number just to confirm. For example, I used the Toyota site and confirmed the housing or “cap assembly, oil filter” as they call it is part number 15620-36020. I could then confirm that number on the Amazon listing. That was good because they didn’t list the XLE trim level in the Amazon post. Sometimes those details matter and sometimes they don’t – in this case it didn’t.
How To Assemble It?
In the Amazon listing, they tell you which of the three lengths of tubes to use. You can also just set your original housing assembly next to the new RJSPHH unit and figure that out in a hurry too.
They do have a brief video and assembly in the video. I watched that and the only thing that threw me for a minute was the actor was holding an o-ring at one point when putting the base plate in that the spring sits in. I’m pretty sure that was a spare o-ring for the small cap that can be removed to drain the oil from the canister first if you want to. You don’t use it when installing the tube.
Summary
This is a solid part. It fit easily with no fitting required on my daughter’s RAV4 and we haven’t had any problems. If you are looking to replace a polymer unit on your Toyota vehicle and are considering this one, I have no hesitation recommending it.
Note, I have to buy all of my parts – nothing here was paid for by sponsors, etc. I do make a small amount if you click on an ad and buy something but that is it. You’re getting my real opinion on stuff.
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Hi folks – back in 2020, I wrote about buying a Mophorn 3 ton pneumatic/air- pillow jack to work on our vehicles. Actually, I bought it in 2019 and it’s still going strong. This past Fall, I decided to get a second air bag jack but decided to get one with a higher lift capacity to better jack up my 2021 Ram 2500.
To give some background, I wanted an air-pillow/air-bag lift for speed and to save my shoulders that could no longer handle pumping a hydraulic jack arm over and over to lift a vehicle. I have an air-over-hydraulic bottle jack but it is tall and slow. The air bag jacks use compressed air to inflate a rubber cylinder that then lifts the vehicle – like what you see in air-ride or air-lift suspensions on trucks. They are called by a variety of names as you can see in this post: pneumatic jacks, air bag jacks, air pllow jacks, pillow lift jacks. Air-over-hydraulic is a different creature – air is used to actuate the hydraulic pump vs. you hand pumping to move the hydraulic pump up.
Always Use Jack Stands
Once the vehicle is in the air, I always put jack stands all the way around to support it. This is always a good idea regardless of jack type you use and the air bag jacks are no different.
There was one thing in their product page on Amazon that confused me until I realized it was a metric term. They say it can lift 11,023 pounds / 5 tons. Well, being used to American measures, 5 tons if 10,000 pounds soI wondered if this was some kind of hype. The issue is that they mean 5 metric tons. A metric ton is 1,000 KG or 2,204.6 so 5 metric tons is 11,023 pounds.
Their stated operating air pressure range is 5-10 kg/cm^2. That comes out to 71.1 to 142.2 PSI. The airline for my driveway tools is at 100 PSI – most of my tools are 90 PSI. My guess is that given their operating range, the jack can’t lift its rated maximum capacity. I can tell you that it has no problem lifting the front or rear of either my 6.7L Hemi 2021 Ram 2500 or full size 2016 Ford Transit F150 van and that’s really what I wanted. The photo at the top of the blog is the Vevor with my Ram 2500 up in the air.
The lifting height is about 15.75″ and the minimum height is 5.3″. The minimum matters a lot when you are trying to get it under some vehicles. One trick I have found is to stand on the air bag to get the air out and then close the exhaust valve to make it thin enough to slide under some cars.
One of the nice perks is that the handle has three positions so you can slide it in flat under a vehicle or at an angle if so you choose. My Mophorn jack’s handle is in a fixed position so that limits how far it can slide under some vehicles but it’s also more sturdy since it can’t move.
With the Mophorn jack, the screws securing the botton of the bag to the plate started to come loose and the unit was leaking air. With the Vevor, they are in solid and really did not want to back off – I was going to add medium Loc-Tite but since they were in so firmly, I decided to leave them alone. They may even have a thread locker applied already – I’m not sure. I think out of all of the screws there were only one or two I could torque down further.
Summary
All in all, the Vevor air bag lift seems like a solid unit. I’ve not had any problems at all. I sometimes wish the handle wouldn’t move so easily but its ability to fold flat to the ground makes up for that.
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Time for a safety briefing and, yes, I am the cause of the briefing. This is not a blame game post – what happened to me will likely happen to me again and may happen to you as well. The important thing is to learn from it because I got real, real lucky.
I was topping off my new Hatsan Jet II with high pressure air from my Omega tank for maybe the dozenth time or more and thought I was being careful. I am respectful of high pressure air because I am a NAUI certified SCUBA diver and sometimes weld right with Gas, MIG and TIG torches. I have heard plenty of stories over the past 40 years (yeah, I am that old) about tanks, fittings and what not. Guess I got sloppy this time.
I connected the DonnyFL female foster fitting to the male foster fitting on the Jet II and gave a gentle tug to make sure it was seated. You always want to do this by the way. I really didn’t think a lot about it because I have refilled from a tank so many times. Bad routines can lead to bad outcomes and it did here.
I was holding the Jet II off at an angle where I could see the manometer (what they call the pressure gauge in the high pressure / pre-charged-pneumatic (PCP) airgun world. I’d guess the angle was about 30-45 degrees and may 18 inches away – these are all best guesses in hind sight.
I cracked open the valve and was doing a slow controlled fill. Somewhere just over 225 bar (3,263) PSI, the hose’s female fitting explosively slipped off the male fitting on the airgun and rocketed off. It happened so fast that I realized my face was numb, I had taken a direct hit in the polycarbonate right lens of my glasses and had heard something like a gun shot. I turned off the air and went to the bathroom to look in the mirror expecting to see blood. I was geniunely surprised there wasn’t any so then I started looking.
My right lens had a gouge where the fitting hit it and saved my eye. I had a small light bruise on my eyebrow but it really wasn’t bad. Luckily, I had spare glasses and grabbed them to be able to see.
What happened?
My next thought was “what the hell just happened?” The O-ring from inside the DonnyFL female quick connect foster fitting was still on the Jet II’s male foster fitting. Nothing had broken – no tears, missing metal or rounded edges.
I was the victim of stacked tolerances. This means that any given specification has a +/- allowance that the machinist can go over or under by and still be ok. The stacked tolerance problem is when you have those tolerances of parts combine to then be outside of specification. Please notice that I am not blaming any of the vendors.
The DonnyFL female quick connect foster adapter, which works fine on my Air Venturi fittings and FX Impact Compact Mk II had slightly different dimensions than the Hatsan male fitting. I had noticed since I first bought the Jet II that I needed to firmly seat the DonnyFL female fitting as it didn’t go on easy. With 20/20 hindsight, I should have realied that was a bad sign and switched to the supplied Hatsan female quick connect fitting. I didn’t make the change befoe because I thought the DonnyFL and was good to go since it worked on everything else. Turns out that was a wrong assumption.
I really don’t know why more harm wasn’t done. Maybe the fitting flew straight out, the end of the hose was reached and it whipped back with less energy. Maybe because my glasses flattened around my eye socket it partially absorbed and then distributed the force. I can tell you I feel real lucky that worse didn’t happen.
What did I do as a result?
All of my air fittings are made by Air Venturi – I buy different configurations of them and keep them in stock so that when I have a fitment problem I can change to an Air Venturi fitting.
In this case, I wasn’t about to take the Hatsan apart so I took the Hastan supplied female fitting and put an Air Venturi male quick connect on the end to get a solid connection both to the airgun and to the DonnyFL quick connect. The fittings go together very smoothly and I’ve not had problem after almost a dozen top offs.
Summary of Lessons Learned
The problem of stacked tolerances will always be around and thus one brand of fitting may not work well with another. So here are the lessons learned.
Be mindful that when you have to push a foster fitting on harder than normal then that likely indicates the fitment is wrong and you must look at your options.
Use the airgun supplied adapter (if they give you one) and then put a brand of fittings on it that allow you to safely mate the parts together if there is a fitment issue.
I will use the pressure gauge on the tank and not the airgun going forward even though I thought I was at a safe angle.
Do not get anywhere near the fitting during refills – especially with your head or face.
I hope this helps you out. It was a wakeup call for me.
If you find this post useful, please share the link on Facebook, with your friends, etc. Your support is much appreciated and if you have any feedback, please email me at in**@ro*********.com. Please note that for links to other websites, I may be paid via an affiliate program such as Avantlink, Impact, Amazon and eBay.